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Greetings to all - I need to correct an incorrect statement: "I will add, by rotating the drive shaft in the reverse direction as stated above, simulates what the kick down switch does by momentarily grounding the ignition system to unload the drive train to allow the pawl to engage the balk ring gear." I SHOULD have stated: I will add, by rotating the drive shaft in the reverse direction as stated above, simulates what happens when the accelerator pedal is released which will unload the drive train to allow the pawl to engage the balk ring gear. Please accept my apologies for any confusion. It's been many years since dealing with one of these transmission so I dug out an R10 OD trans and actually performed the bench test as stated above just to make sure the procedure is true and it is.
64F100 57FAIRLANE500
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I believe the handle on the dash should be pushed in, that is, the OD not locked out. Otherwise, if locked out, the pawl is deliberately blocked outward by the shift rail and can't be pushed inward. So, with the OD enabled and the trans in neutral, pull the pawl out as far as it will go. Then, rotate the drive shaft in the normal direction to set the blocker ring in a normal position as if the car is traveling down the road. Now attempt to push the pawl inward and while holding this inward pressure on the pawl, rotate the drive shaft in the opposite direction and within a few degrees of rotation the pawl should slip off the balk ring and then engage the next slot in the balk ring gear. If this happens, the drive shaft should lock up. That is, you will not be able to rotate the drive shaft in reverse any further when the trans is in OD. I will question once again that when the OD is NOT locked out, the OD shift lever on the side of the trans should be moved back towards the rear of the vehicle. Also, it is correct that the pawl should travel about 1/2 inch from outboard to inboard and outboard again when engaging into the balk ring gear. I will add, by rotating the drive shaft in the reverse direction as stated above, simulates what the kick down switch does by momentarily grounding the ignition system to unload the drive train to allow the pawl to engage the balk ring gear. This is how I bench checked these transmissions after assembly. That's pretty cool the tool you fabricated to manipulate the pawl. Hope this helps....
64F100 57FAIRLANE500
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I now have a working OD solenoid that I removed from another one of my cars. All of the OD electricals check out as good. After struggling with this problem for weeks and reading a long series of posts on "Ford Barn", I am convinced that my problem is mechanical and not electrical and caused by misalignment of the blocker ring with the pawl. The blocker ring must have rotated out of alignment with the pawl when I had the solenoid removed in the past. This problem is described on page 10 of the Borg Warner manual. I tried the remedy for this condition with the solenoid loosened but it didn't work. I made a tool to grab the pawl and push it inward with the solenoid removed while rotating the driveshaft by hand but I only feel about 1/8" movement of the pawl and I don't feel it dropping into the blocker ring no matter how many times I turn the driveshaft. Can someone give me a detailed description of how to realign the blocker ring without pulling the transmission and taking it apart? Should I have the OD dash handle in or out? Should I have the car in a forward gear or in neutral? I assume that the rear wheels should be off of the ground. Thanks
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Allen, I replied to your PM.
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PM sent. Thanks Ford Dearborn!!!
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Allen I get it, you just want to put this problem to bed for good. However, if VanPelt doesn't have one, I wouldn't mind having a look at you old solenoid for the cost of shipping....
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Thanks Dearborn and Daniel. What you are saying makes perfect sense. I think that I am just going to buy a new solenoid from VanPelt rather than continuing to fool around with this one. When the OD problem first started, (the second time) I removed the cover and found it full of trans oil. I cleaned it up and installed a new seal in the transmission and that fixed the leak but the solenoid never worked again when installed although it bench tested OK. Maybe the oil damaged one of the coils???? I will post again after I see if the new solenoid solves my problem.
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alanfreeman (9/27/2024)
I am still having the same problem with my overdrive solenoid. It works when bench tested. However, when I install it and tighten it down it doesn't click when power is applied to the blue wire. I know that I installed it correctly in the trans pawl as before installing the mounting bolts I turned it to the correct position and I could feel the plunger engaged and I could not pull the solenoid straight out. However, if I back the two mounting bolts out and loosen the solenoid it then works when power is applied. This really makes no sense to me but I am at the point where it looks like I will just have to invest in a new solenoid. Any more suggestions? Years ago, when I was testing NOS 6V solenoids, I built a jig to mount them (putting solid resistance against the plunger). Some would bench test fine, but not in the jig. I assumed that when they wouldn’t function properly after the dealer mechanic installed them, they went back on the supplier's shelf (instead of to the manufacturer), and eventually ended up on eBay. Was easier then to just try another, rather than disassemble & repair, though the supply is likely dried up by now.
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It might be that the pullin coil is not functioning but the holding coil is. When the solenoid is on the bench the holding coil is supplying enough force to extend the plunger. The pullin coil is grounded through a contact within the solenoid itself and that contact could be simply dirty or oily etc.. I assume this is a 6V coil. Normally, with a digital ohm meter there should be a very low reading through the blue wire. Something like .3 ohms. A 6V coil should be about 4 to 5 ohms through the holding coil. If you measure through the blue witre with one probe and the other probe on the solenoid frame and get aprox. 4 to 5 ohms , then that would prove the pullin coil in not functioning. Just one possibility since the O/D was working good, then failing intermittently until complete failure. If you should get into the solenoid and find the pullin coil is bad or the contact is toast, I would be glad to pass on a "parts" solenoid to you. Hope this helps and good luck....
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I am still having the same problem with my overdrive solenoid. It works when bench tested. However, when I install it and tighten it down it doesn't click when power is applied to the blue wire. I know that I installed it correctly in the trans pawl as before installing the mounting bolts I turned it to the correct position and I could feel the plunger engaged and I could not pull the solenoid straight out. However, if I back the two mounting bolts out and loosen the solenoid it then works when power is applied. This really makes no sense to me but I am at the point where it looks like I will just have to invest in a new solenoid. Any more suggestions?
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